Solution
The refinery engaged our team to plan and design a wastewater reclamation process to reduce withdrawal of raw water from an aquifer. This included piloting membranes to evaluate scaling, transmembrane pressures and long-term operational costs.
The facility includes multiple cooling water towers and a boiler system for steam production. Both systems require treatment before water use. Piping and valving were designed to allow the refinery to manage the water sources and to use higher quality raw water sources for the boiler feed systems and the lower-quality sources for the cooling water.
Several water sources are now blended and routed to the new treatment facility. The water for the boiler feed system includes chloride remediation wells and fresh groundwater wells. The water for the cooling tower consists of fresh groundwater, secondary domestic effluent and refinery wastewater.
The cooling water system was designed for a permeate future capacity of 2,300 gpm, while the boiler water feed system was designed to deliver 1,500 gpm of permeate.
Other project features include a 4,800-square-foot building for electrical service, operations and instrumentation, and an associated 10/11.2 MVA substation with four transformers.